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0-30 Vdc Stabilized Power Supply


Sallala

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Hi Sallala,
My Microsoft IE6 browser opens pics using my ACDSee viewing program that shows many file types.


- My fuse (5A) at the secunder side of the transformer glowed.

See second-breakdown below.

- T3 went out

What is T3? What happened? (shorted or open)

- Fuse at the output (5A) desn't damaged

If you have a fuse for the output, it should be inside the negative feedback loop to keep the good voltage regulation.

I use only one 2n3055 at this time, with heatsink and a big fan. This worked with no problem.

Maybe it had second-breakdown with such a high strain on it. I bet its chip 's temp exceeded 200 degrees C and it began melting. :'(
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Audioguru:
Something wrong in my workplace's internet access. I can't see any pictures attached to the forum at work. At home everíthing fine  ???
But it's doesn't matter.

I'm sorry: T3=Q3
(In my country, Transistor=T)

Huhh, I checked it, but I don't remember exactly. It wasn't conduct between E-B or B-C. But I'm sure: the LED was bright always. Even if the supply was in constant voltage mode.


If you have a fuse for the output, it should be inside the negative feedback loop to keep the good voltage regulation.


Hmm, of course. As the diode, that you drawed. I must to modify the PCB.
But this is not makes a problem, if the fuse at the output glowed, and it's in the negative feedback?


Maybe it had second-breakdown with such a high strain on it. I bet its chip 's temp exceeded 200 degrees C and it began melting


But how can it's temp exceed 200 degress, when I turned down the votlage potentiometer?

As I wrote, while I working, tha supply was good, and Q2 wasn't too hot.
Then I leave the 2Ohm load at the output, but turned down the voltage potetntiometer.

When I go back, fuse at the bridge rectifier burned.  :o

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T3=Q3

A BC557 operates well within its ratings here. You must have had a weak one.

But how can it's temp exceed 200 degress, when I turned down the votlage potentiometer?

With a positive unregulated supply of 40V and 6V on the output at 3A a single 2N3055 must dissipate 102W. It is rated to dissipate 115W when its case is held at 25 degrees C somehow. If yours was only warm then it was too hot inside. Beginning to melt.

As I wrote, while I working, tha supply was good, and Q2 wasn't too hot.
Then I leave the 2Ohm load at the output, but turned down the voltage potetntiometer.

When I go back, fuse at the bridge rectifier burned.

When a power transistor gets too hot inside, it leaks a lot of current that turns it on harder, making its output voltage to rise, making more heat..... Thermal runaway. 5A into 2 ohms is only 10V. The output probably rose higher, causing more than 5A and blowing the input fuse. A single 2N3055 is not enough for this project.
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  • 2 weeks later...

Hi Smokey,
Welcome to our forum. ;D
This thread discusses modifications to the original project to make it work properly.
I posted a revised parts list in this thread that has a TIP31A real power transistor replacing the little 2N2219, a 30V transformer and two 2N3055 output transistors etc.

In this thread we also discussed that the supply voltage for the opamps is about 49V which far exceeds the absolute max voltage rating of 36V for ordinary opamps like the TL071 or TL081. There are a few opamps with a 44V rating but I recommend using OPA445AP opamps that have a 90V rating.

Many members have made their own pcb and maybe somebody will sell you one. ;D

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The pcb is about the same as the original. Some resistors are larger but must be stood-up from the pcb to avoid charring anyway. The driver transistor Q2 has a different pinout than the original 2N2219 but needs to be mounted on the chassis as its heatsink. A big rectifier bridge replaces the original rectifiers but it also needs to be mounted on the chassis. The original pcb will be fine. ;D

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Hi to you all
first i would like to say that i'm new here, and this site & forum are great!

I would also like to build this PSU, but i want to make it DUAL.
in order to reduce cost/dimentions i would like to know if i can share the whole
area within the red line...
if not, please tell me which compenents I can't share
thanks!

P.S. if there any more sharable components outside the red line please do tell me

post-13545-14279142460724_thumb.jpg

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1) replace Q2 with TIP31A (by the way, can i use B or C instead? i can't find the A type)

B and C are fine. They are rated for higher voltages.

2) add a fan and supply it from a 12v Zener and a resistor OR add another 2N3055, which solution is better?

The current gain of power transistors drops at higher currents and some are weak anyway. Your 4.1A transformer can power this project to produce 3A output if you use two 2N3055 transistors with emitter resistors and a pretty big heatsink. You can reduce the size of the heatsink if you use a fan.

3) replace the 4 1N5402 with a 4A+ bridge rectifier (is it really needed to connect this one to a heatsink?)

With 3A going through it, a bridge rectifier module gets pretty hot without being bolted to the side of a metal box, with some thermal grease.

I really don't care much if this unit won't supply exactly 30v or 3A.
my requierments are 0-24v 2mA-2.5A. will the current circuit plus the changes i described be enough for this?

It will have more output voltage at 3A if R15 is changed to 100 ohms.
It will regulate the voltage better using a BZX79C5V6 zener diode for D8 and 1k for R4.
C1 should be pretty big, about 12,000uF.
R7 should be about 10W.
R2 and R3 should be 2W.
The opamps should have a higher voltage rating than ordinary ones but not as high as the opamps needed with a 30V transformer. With your 24V transformer then MC34071 opamps are fine.

this topic got me really confused....

Yeah, I wish its designer got it right in the beginning.
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Q: does the PCB on the site fits the version you just described?
for example:
1)does the MC34071 have the same pinouts as TL081 so that i can just use these instead?

Exactly the same.

2)do any components need to be stood-up?

R2, R3 and R7 will probably need their wires bent around under them. C1 can be mounted on the chassis with a clamp.

I also have two 10000uF/16v caps, can i connect them in parallel to get 10000uF/32v and will it be enough?

No, No! Two 10,000uF/16V caps in parallel equals a 20,000uF/16V cap. If you put them in series their value is halved to only 5000uF and the one with the lowest value will have more than half the voltage. Also their effective resistance is doubled. Buy a proper capacitor.

I used another cap for testing and the transformers secondary winding voltage doesn't exceed 30v.

The transformer's voltage will rise maybe 1.5VAC with a low-current load. The root of 2 times 24V = 34V peak. The rectifier bridge will have a voltage drop of 1.3V at low load current resulting in a DC voltage of between 32.7V and 34.8V. Add as much as you want for transformer tolerance and mains voltage fluctuations. Use a 50V cap. ;D
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Hello dear all:

    Today I have finished the power supply circuit. But now I have a problem that's when the circuit is power on and adjust limit current. The limit current adjust range
only 670mA ~ 3.92A. The limit current should be 2mA ~ 3A but my circuit is not. When I found the current range is 670mA ~ 3.92A,U2 output (pin 6) voltage range is about 1.5V ~ 4.*V. Is the voltage range correct? If anyone ever has this problem,please tell me that's why. Or you have any suggesion tell me please,too. Thank you very very much.

Best Regards,

            Stanley

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Hi everyone,
i have just finished this supply, i have used all modifications mentioned in this forum except change of opamps. Btw, doubled 2N3055 is REALLY good idea.
All is working fine, i have only one problem and don't know if it is problem in construction or in design. If i turn the PSU on, there is huge voltage peek. For a moment the transformer output voltage appears on output (my is 28V). If i turn the PSU off, than i have about 35V on output and is falling down (as C1 discharges). When the PSU is turned on, it operates normally. Oh and R2 gets sometimes little bit hot (maybe someone can explain me why the combintion of R2 C2 is here, and connected directly to transformer output)

Thanks fo replies
(sorry for my English)

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If i turn the PSU on, there is huge voltage peek. For a moment the transformer output voltage appears on output (my is 28V).

Hi Pigster,
Welcome to our forum. ;D
It sounds like the negative 5.6V supply comes up to its voltage too slow. Maybe R2 is burnt and has increased from 82 ohms. More info about R2 below. The negative supply connects to U2 which controls the output voltage.

If i turn the PSU off, than i have about 35V on output and is falling down (as C1 discharges).

Q1 is supposed to conduct when the project is turned off and then it will immediately drop the output voltage to zero. The negative supply has low-value capacitors that discharge much quicker than C1, therefore Q1 becomes biased on.

When the PSU is turned on, it operates normally.

Great! ;D

R2 gets sometimes little bit hot

Other people said the same thing so I changed its rating to 2W.

maybe someone can explain me why the combintion of R2 C2 is here, and connected directly to transformer output

The negative supply is a standard half-wave charge pump circuit. C2 charges through R2 and D5 when the transformer terminal is positive, then discharges through R3 and D6 into the zener and opamp negative supply pins when the transformer terminal is close to ground.

post-1706-14279142461943_thumb.png

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Hi Stanley,
It sounds like the negative 5.6V supply at D7 isn't working.
U3 is the current comparator and its output needs to be able to go to a negative voltage in order for D9 to pull the output voltage down when the current through R7 exceeds the current setting.


Dear audioguru :

    If D7 isn't working,the vary with voltage (0~30V) will be exceptional. Isn't it? But I still
follow your suggesion to check D7 voltage on my board. The result is -5.50V. Besides I found Q2 bias-emitter voltage is 0.61V,Q4 bias-emitter voltage is 0.63V,R15 voltage is
0.06V(exceptional voltage) when output short. How about your opinion?

Best Regards,

                Stanley
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Hi Stanley,
Your negative supply is fine. ;D
Maybe your R17, R18 or P2 has the wrong value. :(
Maybe your opamp U3 is damaged. :(

Look at my sketch of the current regulator U3 section without any load current, and think about P2 turned down:
1) The opamp's inverting input pin 2 is 0V.
2) The opamp's non-inverting input pin 3 is only +5.6mV.
Therefore the opamp's output is high and it doesnt do anything until the load current is about 12mA (12mA x 0.47 = 5.6mV) and the circuit will keep the load current at 12mA even if you short the output.

Now turn-up P2 a little, increasing the voltage at the opamp's non-inverting input pin 3, then the load current must be increased for the voltage across R7 and at the opamp's inverting input pin 2 to exceed the voltage on pin 3, for it to regulate the load current at this new current.

It is a little more complicated because the output 0V goes positive with respect to the rectifier's and filter's ground with higher load current and the 11.2V reference also goes higher by the same amount, increasing the voltage across the voltage divider with the P2 control.
Understand? ;D

post-1706-14279142462266_thumb.png

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Thanks for explaining negative circuit,
about the peek problem, i have checked all components in negative part, all is ok including 82 ohms R2. I have also done little experiment, i have connected LED to output of PSU, set voltage to about 1,8V, all is fine, LED is ligting, then i have switched off the mains switch and .... amusing efect happened as LED burned out.
Any ideas?

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I said it before.
Quote: "Q1 is supposed to conduct when the project is turned off and then it will immediately drop the output voltage to zero. The negative supply has low-value capacitors that discharge much quicker than C1, therefore Q1 becomes biased on."
Maybe your C1 is defective and its value is much too low.

Does the project still have a huge peak voltage when it is turned on?
C1 having a low value might cause it.

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